In work with lots of WD40 and some bashing and pulling we managed to get two of the studs out from the downpipe flange. The other two wouldnt budge so we drilled and retaped the holes. I have replaced these with stronger studs so hopefully the same problem won't occur.

The boss was very badly damaged so we retaped it first but the sensor seemed a very loose fit due to taking out the other sensor it must have striped a good bit of material. To combat this we drilled out the threads and machined a stainless sleeve which was put it. We then welding this in place and drilled and retaped the boss to the required size leaving a nice clean thread for the new sensor.

We put up both the head face and downpipe flange on the grinder to clean up the faces. Securing the job was quite hard and we only took a couple of thou off as I didnt want to strip too much material. The face doesnt look too good but I am hope the new gasket will seal the edges. I just didnt want to remove too much material from the top.

I got the sensor from eliseparts and hope this one lasts a bit longer than two months. I was just a bit worried of the open wires whether I should use a heat sheilding on them or I would get away with cable tying them away from the manifold to prevent them melting.

Anyways I ordered the gaskets and should hopefully arrive tomorrow and get it swaped over, hopefully the task won't be too hard and the old manifold comes out ok.

I shall keep you updated
